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Broken bolt in my k04 turbo, how best to fix this?

7.3K views 14 replies 9 participants last post by  Hirnbeiss  
#1 ·
So I had a crack in my exhaust manifold (kinetic motorsports high flow exhaust manifold, terrible product, don't buy) and when I took it off to replace it, one of the three bolts connecting the manifold to the turbo had broken off and is now stuck in the turbo. Already tried the ez out bold extractor (broke the tip in the bolt) and tried welding pieces to the bolt. Nothing has worked and I think it's going to get drilled out.

So I can have it drilled out for around $100. My question is can I replace that part of the turbo with a k03 piece or is the k04 different?
 
#3 · (Edited)
Well that's a bummer but good to know, thanks. The bolt broke off below the surface so I think I'm going to have to try to have someone drill it out.


So any hints on taking this thing apart. I need to separate the housing from the turbo. I've loosened a few bolts but they seem too long to unscrew completely. I'm sure it's simple but I need some reassurance before I destroy my turbo further.

edit: I got it apart, just for others taking apart a turbo for the first time, you do just keep unscrewing the six bolts. Unscrew them all until the top of the head hits the metal (I think 3 of them did this) then unscrew them evenly and it forces the housing apart. Tap it on the cement and it popped off for me.
 
#8 ·
It's a bit too late for me to say this, but you could have had somebody weld something to the top of the bolt and take it out that way. I had this problem twice. The first time, the bolt was drilled out (I had no luck with helicoils, and eventually had to replace the whole housing). The second time, my friend's dad helped out by welding a piece of metal to the top of the bolt and taking it out that way.

From that point on, I made sure I used anti-seize on those bolts.
 
#9 ·
Broke a bolt on this bad boy. Its sticking up a little. Have hit it with PB Blaster and Heat, nothing else done yet.



I don't have a welder. But was thinking to try Vice Grips first. Then to try drilling and removal with this left thread bit.



Anyone else have an idea?
 
#11 ·
If you have access to get a drill on it that should do it. A lot of times the heat and vibration from the drilling as well as any 'shrinkage' when the center of the bolt is missing will allow the extractor to just pull it out. In my limited experience, if you have clean access to drill the hole you should be fine.

Vice-grips would probably be quicker so try that first. You can also tap it (a lot.....like 100 times) and use lots of penetrating oil. Plus give the oil time to do its job. I'd oil it, tap it 50 times, then repeat that every day for a few days then try vice-grips. If that doesn't work or you can't wait, drill it out.
 
#12 ·
sorry but mis-read 8 year old post, O.K. first things first, it is a bolt and not a stud. Bolt is therefore not bottomed out in hole versus a stud which stops or as threaded area either hits the bottom of hole or stud runs out of thread.......pretty sure it is 10mm, cannot recall pitch, think 1.25. Assume is did not move at all when trying to remove. The threaded area of the bolt and threaded hole are only touching/make contact on one surface there is a gap on the "bottom side/edge " of the bolt threads and "top side/edge" of the threaded hole. Take a 1/8 or 5/32 inch drill and after center punching "steer" the drilll by eye as close to center,and once centered and perpendicular drill clear through bolt ,you'll feel it when it gets through bolt,heat up and spray B'laster in hole (safety glasses please) you do not have to get real hot, let cool, repeat,repeat Let "digest" couple hors........next take a hammer and give it a good strike on head,well whats left. this will drive bolt away ever so slightly from torqued/binding surface. then vise grips...... now if this fails, using hole you just drilled, using correct size drill, size hole for an easy out , too big an easy out will make it worse as the taper on it will expand bolt,too small and if easyout (which are harder than hell) breaks off flush , you will have to get it EDM'ed out. Now if easy out does not does not work, progressively drill hole to 11/32, just threads should be left, re-tap and ready to go.